I took Hazel for a ride back up to York this morning. The plan was to pick up an NOS fender and the black rear seat from the guy I’d visited last weekend; my friend Mike mentioned on Instagram that he was interested in the fender so I thought I’d head back up, grab that and the rear seat I spied last week. It was a balmy 50˚ so I was happy to only need a fleece for the whole day, and the sun peeked through clouds that began to darken the western sky as we got further north.
The guy who owns the lot wasn’t available so I had another guy take me where they had the fender stored. It looked OK under the lights—dirty on the inside, a few scratches on the outside—and all of the bolt holes were clean (except one which held a rusty nut/bolt combination; clearly he’d had it mounted on the truck at some point) so I threw it in the car.
We needed some PB Blaster to get the hinges on the seat to move—they were frozen, probably from sitting outside for weeks on end. But when I was able to get it to fold, I was sold. I headed back to the shop and paid the money, took some pictures of some old British cars he had on the lot, and hit the road.
On closer inspection when I got the fender home, I wish I’d been more careful. After really cleaning off the dirt on the inside, my heart sank. It’s NOS but at some point the owner had let it sit, probably inside-up, where water had pooled and started a layer of rust bubbling on the lower edges. It’s not all the way through, and could easily be cleaned up with a soda blast or some other abrasive, but it’s not a perfect fender. I’m going to send Mike a video I took with the detail and show him exactly what I’ve got here to see if he’s still interested. Mike specializes in show-winning restorations, and this might not be up to his standards.
The lesson here, which I’m still trying to learn at my age, is: slow down and be patient. Check over everything before you pay the money. If Mike doesn’t want it, I won’t be terribly upset; both of my other spare driver’s fenders are probably at best a 6 out of 10—the brown one I got last year might be a 5, and I paid next to nothing for it. I’ve also got to look at my parts scores on the whole: most of what I’ve gotten up until today has been very cheap. This is the most expensive part I’ve bought for the truck since I’ve had it, and it’s as closer to new than any other Scout parts I own besides the two lights from last week. So maybe it all evens out somehow…?
After I got home and got some lunch, I headed out to the garage to clean the heater box up. Now that I’ve got a proper sandblasting cabinet, I figured it wouldn’t be messy, but I had to do a bunch of prep work to get it ready.
First, I drained all of the sand out of the bottom of the cabinet and stored it in a bucket. The cabinet came with a gravity feed hose—basically as long as the bottom of the cabinet is full of sand, it sucks the sand in and mixes it in the gun at the tip, making it a closed system. But the tip it came with was broken and the Eastwood tips are larger than my Harbor Freight tips, so I figured I’d use what I already have. Propping the cabinet up on a box, I replaced both of the lights inside and filled my compressor. Then I loaded up my little HF canister with glass bead and got to work.
It did a really good job once I got the flow dialed in, and I a good bit of the box clean before I had to sieve the blasting media for big chunks that started clogging the tip. I also had to take frequent stops because the inside of the box isn’t properly vented yet—I need to get a hose with some kind of pusher motor to mount on the back to vent the dust out—but I got a lot done before the valve on the HF “gun” blew out on the side. It’s basically just a 3/8″ ball valve, not meant for abrasive use. After cleaning it up, I looked over the Eastwood gun and figured I’d give it a shot with the broken tip to see how the flow worked. I dumped the sand back in, hooked it up to the compressor, and was shocked at how well it threw sand even with a broken tip. Clearly the simpler system is the way to go, so I’m going to source some new tips from Eastwood and use that to finish off the parts.
When I was done with that I cut some lumber down to make a rolling cart for the cabinet with a shelf on the bottom, and with the addition of some HF casters I had it assembled and the cabinet on top in about 45 minutes. A panel on the back will keep it from being wobbly.