Floorpan, Continued

I spent a couple of evenings this past week breaking down the green Travelall doors and collecting all of the parts to see how things look. The passenger door is in worse shape than the driver’s; there’s a fair bit of rust-through under the wing window on the bottom. Both doors are down to the metal, but on each one the lower hinge needs to be drilled out. That may make reusing them both tricky, but I think careful screw removal and re-tapping the hole is possible. Both windows, scissor assemblies, latch mechanisms, and most of the window channels are all in good shape. I’ve also got a second set of pre-’65 door latches for both sides from my friend Don in Ohio, which will come in handy as spares in case I need them.

The other thing Don sent me was a spare set of IH mirror assemblies. One of them is basically just the bracket, but the other held the mirror housing (minus the mirror) which actually worked in my favor, because I can see how the interior parts are assembled. Essentially there’s a long rod that goes through the center, threaded at each end, and held in place with two brackets welded to the rod. So even if I wanted to pull the rod out of my good housings I couldn’t.

To recap, the threads on one of my good mirrors was so rusted the bolts snapped off on each side, leaving me with no way to attach it to the bracket. Pretty much the only way I can make my good mirror work is to carefully pull one of the endcaps off, pull the threaded rod out, and replace it with a new one. The rod is pretty simple; it’s 1/4″ and takes a 1/4″ – 28 thread, which is easy to find a die for. It’s getting the cap off that worries me. It’s thin steel over an aluminum housing, so I have to be very careful taking things apart.

Saturday I stopped in at a neighborhood estate sale and picked up $20 worth of brand-name used tools that will come in handy for backups and spares, including four vice-grips and several wrenches.

Sunday I got back out to the truck and continued cutting and welding new metal in to the passenger’s footwell. I wound up taking more metal out, as I was having blow-through issues with bad metal and finding some pinholes as I was cleaning other sections. I think I’ve got all of the bad stuff out, and the stuff that’s still mildly pockmarked just got a thick coat of encapsulator. Underneath I ground out the rest of the welds and got it ready for paint. All of this took the majority of the day, as I was doing a lot of cutting and trimming, which sent me back and forth to the bench grinder.

The paint cured overnight and is now ready for seam sealer, which will be applied liberally around the edges before everything gets primed. On the outside edge of the footwell I ground everything flat and covered it in etch primer; it’s going to get several coats of chassis black and then a layer of undercoating to keep out the water.

Finally, I used some vinegar to flush out the inside of the gas tank and let that sit for a day and a half , shaking it around inside to get the crud out and neutralize any rust. Running a borescope down inside the tank, it looks shockingly clean apart from the remains of mud dauber nests. I flushed it with water and a solution of baking soda, then flushed it again and set it out to dry. The outside was covered with undercoating and some surface rust along the top and sides, so i hit that with a wire wheel and quickly got the whole thing down to bare metal. When the top and sides were clean I covered the trouble spots with Encapsulator and the bare spots with etch primer. I’m back and forth about pulling the fuel sender, but leaning towards leaving it in, as I know that it works and don’t want to mess with that.

So in the next couple of days when the temperature gets above 60˚ I’m going to apply sealer and paint to button up as much as I can.

Posted on   |    |  Posted in Purchasing, Welding

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