Leaky Gasket.

I took the Scout over to some friends’ last night to pick up a load of baby toys, and figured it would be a good idea to put some gas in the tank. There’s something wrong with either the gas gauge or the sender in the tank, because it’s never registered anything other than empty. As I started to pump, I noticed gas splashing down under the axles and immediately stopped. From what I can see, there’s a rubber hose connecting the steel fuel tube with the side of the tank which is splitting and pissing everything directly onto the ground.

Not to be discouraged, I continued on to my friends’ house (a few knocks on the tank verified there was sufficient gas available) and made it home alright. But now I’ve got to source a hose that won’t disintegrate with exposure to gasoline.

* * *

Last weekend I removed the entire soft top and folded it carefully for storage in my basement, along with the door frames, bed rails, and hoops. With soft tops being scarce and expensive, I’m going to try and keep this one in good shape for as long as I can. I replaced it with the bikini top, which went on easily, although I’ve got to add a tiedown on the driver’s side and redrill the holes at the edges of the windshield to secure the rail. This is the first time I’ve had a bikini top, and I have to say, it’s very nice.

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Progress on a Scout (not mine, part 2)

This morning I dropped by Mr. Soundman’s house to lend a hand in de-tubbing his Scout. He has a 1972 with relatively clean sheetmetal but a frame that’s seen better days. His plan is to add his good parts to a donor frame to make one clean Scout.

Before, take 1

He’d gotten everything off the tub prior to this morning, and soaked the body bolts in WD-40 to make for easier removal, so we got right to work. The body bolts came off, the steering linkage was removed, various electrical connections were removed, and the tank got drained and dropped.

Then, it was Miller time.

Before, take 2

The next step was to get it as close to its final destination as possible so as to save our lower backs from years of chiropractic reconstruction. After removing a length of fence, we angled the truck out of the carport and into the backyard within a stone’s throw of a flat concrete pad. Experimentation with 2x4s and leverage determined that we needed to lower the front of the frame to get the tub high enough to clear the transfer stick, so we removed the front wheels and lowered the body onto jackstands.

Moved into the yard

Once that was accomplished, we heaved the tub off the chassis and the four of us got it over to the concrete with only one (hopefully) minor strain. Boy, was I glad that went quickly, and surprised at how much that thing weighed. Note to self: this is a 6-man job.

Success!

Then, it was a matter of redoing what we’d undone to get the frame back on four wheels and into the carport. A little shoving, a little kicking, and the chassis was under cover for the evening.

Chassis ready to move

All in all, it was a very successful day—the four of us got a lot done in five hours.