Right In The Feels

This old girl showed up on Barnfinds.com today and it hit me right in all the sensitive spots. This rig is an exact copy of Chewbacca back in the day, except for the Diesel badges on the fenders and the license plate arrangement on the tailgate. Like this truck Chewbacca was a 1978 painted Siam Yellow with no exterior trim, had all four stock hubcaps, a color-matched traveltop with no roof rack, and inside was the same Tanbark high-back bucket seats, rubber floor mats, green accents, and 4-speed stick. Chewbacca had regular side mirrors and BFG Mud-Terrains. The example for sale has some serious rust in the rockers and quarter panels, some road rash and there’s a Nissan diesel under the hood, but if I squint just a little bit I can see ol’ Chewbacca parked out in front of my house waiting for another trip to the beach.

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Shiny Red

Jeff gave me a ring early in the week and asked me to send him the existing overs off the seats I have because he’s worried what he has might not fit correctly. So I went out at lunchtime on Tuesday and quickly pulled the covers off the rear bench and front vertical section, wrote where they came from, and boxed them up to be UPS’d up to him. I would like to have spent more time taking pictures of how they were assembled, but I was up against the clock and weather, and wanted to keep the process moving.

Jeff said I’m welcome to come up to his place and he’d show me how they go together when he’s got them completed, and it’s looking more and more like I might take him up on that offer. I’m sure I could figure out a lot of things on my own but I’d rather have an expert show me the right way first before I ruin anything.

The other thing I did on Saturday was to cut and fit two sections of steel to the corners before welding them into place. I have no idea why they would have kept these parts separate, and I figured sturdier is better in any case. A spray can of Rust-Stop helped me reach all the sections the brush missed, and with that the front bench is ready for upholstery. Next I’ve got to clean off the rear.

On the fender I got all of the low spots mudded out and sanded down, then used fill & sanding primer to identify any last trouble spots. When I was satisfied with the way things looked I used some 1000 grit to polish it up and then sprayed on two coats of rattle-can IH Implement Red to cover things. Overall it looks very good, and there’s only a drip around the fuel inlet port I have to smooth out. The next step will be to scrape all the old undercoating off the back, wire wheel any remaining rust, cover it with Encapsulator, and then spray on some undercoating.

I took the driver’s side off and started knocking off all the Bondo I’d applied in the summer as well as the stuff it came to me with; I’m going to take it back down to bare metal and start over again. This time I’m going to cut out the bad metal and riveted patch and try to get it as close to the original as I can while I keep looking for replacements. This one is going to take a lot more time to fix.

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Compression

Saturday morning broke with the first good sunshine we’ve had in a long time, so I decided that I would take advantage of as much of it as I could. After a mile-long walk with the dog and a cup of coffee with Jen, I put on my coveralls and headed out to the garage. The first thing I wanted to tackle was pulling and inspecting each spark plug I’d installed last year to ensure they were gapped correctly and to do a compression test. I pulled the coil wire, started with the #1 cylinder and worked my way backwards on the driver’s side, then finished on the passenger side.

All of the gaps looked right at spec, and the tips were all covered in gassy-smelling oil—which I expected, considering that I haven’t been able to get her running consistently for a long period of time. The most important information was good information: all of the cylinders had excellent compression, with the lowest of any of them at 125psi. This means the rings are in great shape and have hopefully reseated themselves after their long slumber.

When that was done I pulled the passenger fender out into the sun and hit it with sanding blocks for the second time, working the high spots down and smoothing out the second skim coat. It’s really shaping up on the outside, and I’m having great luck with the new filler.

One drawback was that the inner metal collar I’d welded on to the backside of the fuel port came off as I was sanding it down; when I welded the inside edges and then sanded off the excess metal apparently I was a little too zealous and weakened those welds. So this time I predrilled a bunch of pilot holes along the outer circumference and used those to tack the collar back in place from the back side—something I should have done in the first place. I’ll fill the inside edge with seam sealer to hide the welds, which are mostly hidden anyway. Then I skimmed filler on the low spots, which are (thankfully) decreasing in number.

Sunday morning I ran up the Scout for the first time in two weeks and let it warm up in the driveway. After attaching my ghetto exhaust extender (a 5′ length of HVAC pipe attached to the tailpipe, with 20′ of PVC reaching past the side of the garage) I turned both idle mixture screws all the way back into the carb and then backed them out 1/4 turn. Adding a little starting fluid to the carb, she fired right up and idled much smoother than she had two weeks ago, but then I saw the giant clouds of white smoke coming from the end of the exhaust and figured I’d better shut her down. So the rough idle issue is mostly sorted out, but I need a good windy day to run it up and clean the Berrymans out of the fuel system.

Next, I got to work tearing the front bench seat base down to the metal. I set up a GoPro and took a bunch of pictures, then started tearing the old vinyl off the frame. Removing the foam, burlap, and reed padding, I cut the old hog rings off and wire wheeled the outside elements, and then looked it over. There were three sections that needed to be welded back together, so I set up the MIG, dialed it in for thinner metal, and put them back together. Then I brushed encapsulator on the whole thing, which was a tedious job.

There are two sections on the back side that look like they could have been welded originally, but also maybe they weren’t. I texted Jeff to see what he thought and he told me his seat is from a ’68 and doesn’t look like mine. I’m mulling over whether I should weld in a set of supports there just to keep the whole thing sturdy.

While that was drying I pulled the fender out and continued sanding the high points down. It’s getting very close. There are only about five small areas that needed to be skimmed—hopefully for the last time—so I put some filler on to cure while the weather was still warm.

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Weekly Roundup, 1.28

Knowing it was going to be warm towards the end of the week, I made a beeline out to the local Eastwood store on Wednesday. They had the body filler I was looking for, a specialty brand that came highly recommended online, and  Amazon couldn’t promise to deliver it before then. I was able to throw in a new can of Encapsulator to meet the minimum for a coupon, so it worked out perfectly. This new filler is lighter and sands much easier, making bodywork much more pleasant. I was able to get the high spots knocked down quickly and then spent time finding the problem areas, marking them out with a Sharpie and readying them for the next skim. I actually covered more areas now that I know how easy it is to work with, and I’m looking forward to getting this piece cleaned up.

I got a call from my friend Jeff on Sunday morning, to ask me a question about my seats, which he’s starting today! He figures it should be a week or so to get them done, which means I need to get cracking on ordering foam and materials. That news made my day.

Meanwhile the Travelall/Travelette/C-series designs I’ve been working on have been getting some decent traction for the last two weeks; I’ve sold about 20 shirts and a bunch of mugs and other stuff. And I finished off the first custom design for a guy in Texas today, which has me thinking about how to take commissions when I get the Scout version working. I’m going to get a little merch produced to photograph and then I’ll use that for the next promotion cycle.

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Slow Weekend

I did a little work on the fender this weekend to get it shaped up for body filler. I had to stop welding midway through  the third patch last weekend, so I plugged everything back in and finished that off today. It’s going to take a fair bit of filler to smooth everything out because I can’t get to the backside to hammer out any of the waves, but I’m not too worried about that. The whole thing is going to take some time and attention to finish off right, but I’m happy with the way things are going so far.

Updating the Travelall to-do list last week I realized I don’t have some of the information I need on the health of the engine, so I spent $20 on a compression tester for when the weather warms up. The last time I started her, she ran very rough, so I think there’s more work to do tuning her up. I’m going to pull the plugs, see how they look, and properly gap them all. Then I’ll do a compression test and put them back in.

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Commerce

I’ve had an idea for a T-shirt design bubbling in my head for a while now, and while I was working on video editing (and waiting for files to render) last week, I put it together in Illustrator:  a profile view of a Travelall with the script I’ve already built underneath. This time I built two designs—one for light-colored shirts and one for dark, which is more work but avoids a pet peeve of mine, when printers just reverse out a design in white and the negative spaces aren’t correctly negative. The other big leap I took was to post it up in a couple of Travelall-specific groups on Facebook, the first time I’ve posted there (other than Marketplace) in years. Within 24 hours I sold seven shirts and got two requests for custom truck colors and one for a coffee mug, which was easy to do because of the way I set the file up.

Here’s to hoping the orders keep coming in; I think I might do a Scout II next—until the VW group sends me a cease-and-desist.

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2024 To-Do List

I spent most of my time in 2023 focused on the Travelall, but there were a couple of issues I sorted out with the Scout; the main one being the exhaust leak. That sort of sidelined her for a good chunk of the summer, but I got her fixed in August. There are a couple of small issues that need to be addressed that I’d like to tackle in the spring:

  • Fix the turn signal canceler. Left turns don’t work but right turns do. Why? Probably because I put the plastic return ring in the wrong position when I reassembled the column. At least now I’m not as afraid to tear into it as I was the first time.
  • Get the exhaust manifold fixed. One side leaking again and making lots of noise; I haven’t been able to figure out which is the culprit.
  • Replace the wing window seals and spring hinge. My wing windows are leaky and loose. The gaskets are dry and brittle, and the spring hinges inside the door are both broken. I have new rubber on the bench in the basement, and I’m trying to assemble two working replacements from the six spares I’ve got (this is more of a problem than it sounds; there are two failure points on these windows and most of mine have fallen victim to at least one of them). I’ll probably bite the bullet and pull the working windows from the truck.
  • Swap the gas tanks. I have the original steel tank Peer Pressure came with, and I’ve heard from several places that poly tanks will never seal at the sender properly. I’m inclined to believe this after eight years of suffering through gas fumes and leaks. Having looked at the inside of the tank and cleaned up the outside, there’s a new sender mounted and ready to go. The next step is grounding the tank and checking the wiring before it goes onto the truck, and then actually swapping it out.
  • Get the spare engine on a proper engine stand. I’ve been saying this for a couple of years now, but I’d really like to get it done. The problem isn’t the stand, but how I can lift the engine up onto it. My garage is in no shape to support a chain hoist or any kind of overhead block and tackle, so I’ll have to borrow an engine hoist from somewhere for a 15-minute operation.
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Manual

I stumbled upon an original 1963 Operator’s Manual for the Travelall on eBay before Christmas but passed on it because I thought the price was too high; eBay contacted me after New Year’s and told me the seller had dropped the price dramatically so I jumped on it. It stinks of cigarettes and old man but it’s in fantastic shape otherwise, and as a time capsule it’s a lot of fun.

In the meantime I went out to warm up the Scout and see if I could get the Travelall running as well. After some initial tests I filled the carb bowl and shot it with starting fluid, and it coughed to life briefly. I noticed that nothing was reaching the fuel filter above the fuel pump, so I threw some gas in the tank and tried it again. This time it ran choppily for about a minute before it starved out again, so I dumped the rest of my gas in the tank and tried one more time with the battery power I had left. Clearly the gas in the tank has evaporated out—I’ve only got the cap to a spray can covering the inlet tube—so I’ll go get some more gas and fill it up before I try it again.

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